The LC Engineering tech suggested that we remove the carburetor, to check that the throttle butterflies were centered. We found that the secondary was not. We also noticed a small casting defect on the throttle body. Further inspection found that the hole went all of the way through, so we had to return the carburetor. I called LC and they shipped a replacement that day. I also emailed Weber. Weber wanted the defective carburetor, so they offered an upgrade to a 38. We had that in our hands the next day!
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Shining a flashlight from in the bore |
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